Hobby-Wing ARRIS X-Speed Carbon Fiber FPV 250 Racing Quadcopter with OSD and GPS has bad wobble and instability on first flight out of the box. It looks like the PID values need tweaked in the CC3D flight controller. Also didn’t get some spare parts and some quadcopter functions agreed upon.
after you re-tune it look to see that your props are balanced.
some can be very bad and right across the range like DAL and gemfan having
average 3 out of ten way off balance. could contribute to the wobble or
bent motor shafts
bugger. thought that could be the problem. hope you get it sorted m8
Thanks. I always balance my props.