Diagnosing an Oscillation Problem with the Martian II FPV Racing Drone. Flight footage shows this Drone Oscillating even at low throttle.
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Components:
Matian II FPV Frame
Hyperlite V3 2206 2600KV
DYS XS30 BLHeli S ESC
HUBOSD PDB
Pyrodrone 200mw VTX
Pyrodrone 650 TVL Block Camera
F303 Flight Controller
TBS Triumph Antenna
RaceKraft 5051 Props
FrSky X4R Rx
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I like that you bring this up (the issue with powerful motors) but I don’t
get it. If the inputs from the FC to the ESCs are resulting in too much
actuation, why don’t just lower P and D?
The one or two times I have upgraded a setup with more powerful motors, all
I got to do was lower P a little. Well, maybe I just never tried really
powerful motors…
hey what’s after those propellers?
Im building a 186mm X frame with zmx fusion x25, racekraft 5051 props,
DALRC 25a BLheli_s esc and Xracer f303 v3.1(MPU 6000)
Since you had issues with F303, which FC do you recommend?
It seems you have mounted the XT60 plug the wrong way……this might
result in current finding its way through the frame and maybe to the
TX……….resulting either hot screws or other faults. Happened to me on
the Alien…….
why don’t yiu update to betaflight 3.0?